You have to be carefull though: One time we used a big wd40 can jubileed into the air filter pipe. It got to about 2 bar and I nearly lost my head as the can shot out of the silicone hose like a mortar round and hit the barn ceiling
You have to be carefull though: One time we used a big wd40 can jubileed into the air filter pipe. It got to about 2 bar and I nearly lost my head as the can shot out of the silicone hose like a mortar round and hit the barn ceiling
Just getting back on this now, got everything I need to to start putting back together and testing more.
I'l keep posting.
Done this - It's amazing how many places it leaked - there are still 2 minute leaks that will need the engine out to sort, but they really are very small, one on the inlet manifold and one directly on the turbo compressor housing. that was at 30psi aswell, at 20psi you couldn't hear a peep.
A few other things checked now.
All valves lift between 9.3mm and 9.7mm
Cam is timed in @ 15deg atdc
the head is 73mm
Compression tests as follows.
1 - 140 psi
2 - 150psi
3 - 145psi
4 - 149 psi
Checked everything bar for exhaust back pressure which I will be doing at the Renault Turbo UK festival. Everything seems to check out fine so far.
Any comments anyone?
Did you check the intercooler? Re what I said further up the post.. Get a boost gauge plumbed in and check how much boost the turbo is having to make for the engine to see the 23psi..
Last edited by TNT ANDY; 15-07-2012 at 21:04. Reason: wer
Plumb my gauge I gave you in to the other side of the cooler Andy, last time I tested the pwr cooler core I think I had very very minimal change, 1psi rings a bell
Damn was worth a check.. One of my mates had the same prob, he changed loads of stuff and the car was still getting slower.. He went to a tuner he use's and that's what they found, the turbo was producing about 60psi and the engine was only seeing 30 lol.. So they looked and found that the cooler had collapsed inside..
Have u tried it without a air filter?
I'm not guaranteeing anything Andy but I'm sure your problem is still cam timing related mate as unfortunately I had this same problem about 7 years ago had someone dial my cam in went on the rollers and for an engine and turbo built at that time should have see about 180bhp it made almost 140 for about 20psi down at glen t of dynotech came back got the cam timing re done again by someone else who showed the cam being 12% out and a few degrees can make a big difference went back on the rollers same boost and found 172bhp And that same cam is what I'm still using to this day which is still finding some good power I really hope you find the problem soon mate
Not since re-timing the cam, we did on my 1st visit to Scoff which made no difference and we where seeing 203bhp then. We simply run out of time last time I was there. Might be interesting to do some more testing now the cam is about right, it might be pulling a lot more air in top end and I'm seeing restriction there now. I'm going to have to leave it now as I can't justify another epic trip to try small things like this. I was out in her last night, and she still feels really quick, I'm not gonna get hung up on this.